Commit bdb3656e authored by Simon Horman's avatar Simon Horman
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arm64: dts: m3ulcb: Fix EthernetAVB PHY timing



Set PHY rxc-skew-ps to 1500 and all other values to their default values.

This is intended to to address failures in the case of 1Gbps communication
using the salvator-x board with the KSZ9031RNX phy. This has been
reported to occur with both the r8a7795 (H3) and r8a7796 (M3-W) SoCs.

Based in a similar patch for the r8a7796 salvator-x by Kazuya Mizuguchi.

Signed-off-by: default avatarSimon Horman <horms+renesas@verge.net.au>
parent d2ae6fed
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+1 −12
Original line number Diff line number Diff line
@@ -169,18 +169,7 @@
	status = "okay";

	phy0: ethernet-phy@0 {
		rxc-skew-ps = <900>;
		rxdv-skew-ps = <0>;
		rxd0-skew-ps = <0>;
		rxd1-skew-ps = <0>;
		rxd2-skew-ps = <0>;
		rxd3-skew-ps = <0>;
		txc-skew-ps = <900>;
		txen-skew-ps = <0>;
		txd0-skew-ps = <0>;
		txd1-skew-ps = <0>;
		txd2-skew-ps = <0>;
		txd3-skew-ps = <0>;
		rxc-skew-ps = <1500>;
		reg = <0>;
		interrupt-parent = <&gpio2>;
		interrupts = <11 IRQ_TYPE_LEVEL_LOW>;